Nederlandse Spoorwegen 7851-7852
The prototype

NS7851 during shunting services on the Rotterdam Feyenoord yard, 1946
These locomotives started their active lives in 1901 as E3/3 type shunting loco's
of the Jura-Simplon railroad, later the Swiss Federal Rails (SBB). During the
second world war the Dutch government in exile made preparations for getting
the economy started again as soon as the war would be over. One of the concerns
was getting sufficient motive power on the rails again. Buying existing surplus
from the SBB was one of the measures. Only two of this type (numbers 7851-7852),
and five of a very similar type (numbers 7801-7805) saw service in Rotterdam.
All seven were scrapped in 1948 as soon as sufficient shunting locomotives were
available again.
Recently a sister engine was bought in Switzerland and
was restored to running order at the MBS
scenic railway
The model

At present this model is still my only Dutch model and it is not even originally
Dutch. It was manufactured by Liliput and I bought it in the late seventies
in Austria. Although the rods and valve gears and many other parts do not meet
today's standards of modeling I still think it is a pretty model.
Reconstruction
This model was was seriously damaged in the collapse
of my bookshelves in the summer of 2006. I set the NS7851 aside for later inspection
but it was very likely a total loss. Among this model two other models were
seriously involved: the Big
Boy, crushed beyond repair and the BRB.
The BRB, though heavily damaged, can be rebuild. The Shay
was also involved but damage was limited, though painful because I had only
recently completed the project. I will repair it when I find the courage to
restart a finished project.
Thankfully other models like my Climax and Y3 went out without a scratch.
In January 2007 I started reconstruction activities.
The first model to undergo inspection was the NS7851. Although I considered
it a total loss, I wanted to try reconstructing for the simple reason that it
was a model I bought in my youth years. It is easy to buy another one, a good
second hand model would cost only 70-90 euro. But emotionally this model is
priceless.
Visual inspection revealed the following damage:
- The superstructure was pushed down and was sitting
lopsided to the back.
- The rear of the engine cab bulged outward because
it was pushed over obstacles belonging to the inner structure of the frame.
- One buffer had come off.
- On the rear both air hoses and the coupling had come
off
- Various handrails were broken
- The cab roof was dented and torn.
- The whistle was completely flattened, quite obviously
beyond repair
- The stack was scratched on top
Second to the visual inspection I attempted to run the
model. The visual inspection was disturbing, but the running trial was seriously
discouraging. A hum was all it produced no matter how much current I applied.
It didn't move, not even a fraction of an inch!!
I started by disassembling the superstructure from the
frame. As it turned out the bulging of the cab rear was caused by a notch on
the frame. The damage proved not serious and relatively easy to repair. One
problem solved.
A second running trial without the superstructure made no difference: it just
wouldn't move.
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After thorough inspection of the frame and after
some simple tricks to get things going,
I started taking the frame apart piece by piece. After every disassembly
step I tried to run the motor.
I ended up with a completely disassembled frame,
wheels off, rods off, cylinders and valve gear off. Only than the motor
would run.
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As it turned out the axle of the rear wheel set
was warped. I had to exert considerable force to straighten it. Of course
it is virtually impossible to bring it back into its original shape.
But I tried as much as I could and dared.
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I spent quite some time on requartering the wheels.
After careful reconstruction it was time to do
running trails. They were satisfying. This model won't run superbly
anymore unless I happen to find a replacement for the rear axle. But
as it is I'm quite happy. Having made it run again is the one major
step towards a successful reconstruction. The loco wasn't a total loss
after all, to my great relief!!
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Next I started reattaching the buffer. This has
been a problem since my youth when the buffer came off after a small
accident. Since then I repaired it numerous times by simply gluing it
back into place. But even ACC wouldn't hold it very firmly.
And now I wanted a definitive solution.
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I cut the stem and drilled a 0,7 mm hole in the
center
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I drilled a corresponding 0,7 mm hole in the
buffer housing on the loco.
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I drove a 0,7 mm brass wire into the hole in
the buffer and secured it with ACC.
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And mounted the renewed buffer in its housing
and once again secured it with a little ACC
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Next was the cab roof. As you can see only the
stubs of the whistle remains. The front edge of the roof was torn and
dented. The rear edge of the roof (barely visible on this photo was
scratched taking away all rivets.
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Fortunately I salvaged all loose parts after
the collapse of my bookshelves. So I retained part of the whistle mechanism.
I remodeled the whistle with a little Tamiya putty, which I drilled
and pierced with a piece of 0,5 mm brass wire.
I cemented the tear in the front edge and filled
the dent with putty. After hardening I drilled a 0,5 mm hole to reposition
the whistle. A very small piece of styrene was used to compensate for
the whistle mechanism falling a little too short.
All right it won't be like it was, but it will
do, certainly after a good paint job. Remember the whistle is only 5
mm high!
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Reconstructing the stack was probably the most
challenging part of the job. I attached some Expoxy Putty to the stack,
let it set and molded it with knife, file and sanding paper
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until it suited me. During the job the putty
came loose since it has only so little grip. I reattached the putty
with some ACC.
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Reattaching the air hoses was, let's say, a delicate
job. With only just tenths of millimeters to spare to all sides I drilled
a 0,5 mm hole
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and inserted a short piece of brass wire.
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I drilled a corresponding hole in the buffer
beam, inserted the brass wire and fixed it with some ACC.
Then I cut the protruding wire flush on the inside.
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There you are. Much better and in near original
state.
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I also applied de the brass wire technique to
the steps under the drivers cab. The left one is not entirely straight
but once painted black this is very inconspicuous.
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The brass wire technique was also applicable
to one track cleaner (is this the rigth term?), but I changed the working
order a little. I first glued the cleaner back into place. After setting
I drilled the hole through the glued connection
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and only then inserted the brass wire to reinforce
the connection.
The photo clearly shows the marginal tolerances
available. Use of a drill
stand in combination with a X-Y-
table is absolutely essential. This is work that cannot be done
by hand.
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A final portrait of the reconstructed and partially
repainted model

Before
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After
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Before |

After |
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